Jeep Snorkel - Make Your Own


Tools:
As Required
Cost: About $60 (Cheap!)
Additional Cost: +$2k (Not so cheap!)
Time: Weekend Project
Difficulty: 3 / 4 - Messing up will
really hurt your wallet, but it’s not rocket
science!
Objectives:
1. Deliver unrestricted, dry, filtered air to
the Engine throttle body
2. To be rugged enough to survive an impact and
extreme weather conditions
3. To be Aesthetic pleasing in appearance
Some Background. I’m not a daily mudder, in fact
hate mud, but I’ve come close to testing the
limits of the current intake system, and it only
takes 2 Tsp of water to destroy an engine. Also,
a cold air system would be nice to have, and I
needed to install the welder too. Snorkel was
the solution. I disliked how Chrysler installed
a plastic maze of intake (Fig 1) , it
took up allot of under-hood space! Additionally,
and every aftermarket snorkel reused the
original intake system. So I went the direction
of building my own system after weeks of
research.

(Fig 1 – Hamster
Habitat)
****Disclaimer: Adding a higher intake does not
automatically make your vehicle water superior,
it only provides engine insurance. Search the
forums on all that’s involved before submerging
your Jeep and the risk involved.****
First objective
was filtered air in a serviceable water tight
canister. There were not many aftermarket
options for canisters; those that were available
blew the budget. I went to a local auto store
and opened all the K&N filters boxes... I found
a desirable K&N filter I wanted and combined it
with a Stainless Steel Paint. The two were a
perfect match, almost more than a coincidence I
feel. (Fig 2) Just these two parts alone
could run independently of everything else in
case of severe snorkel damage from a roll-over
or fire. Built in redundancy!

(Fig 2 – Filter
applied and roughed-in for fit)
I found 8 clips, which were bolted to the side
with lock-nuts and lok-tite. A dried RTV Bead on
the opening provided a permanent reusable
gasket. The elbow is ABS, and the OEM rubber
collar connected it to the Throttle Body. A hole
was tapped on the Elbow to allow filtered
Crank-case ventilation. (Fig 3) The face
(bottom of the can) was reinforced with a layer
of sheet metal and RTV for impact strength due
foreign objects projected by the fan. Several
layers of paint were applied inside, and out, to
inhibit rust from forming.

(Fig 3 – Canister Assembled)
Second Objective was to figure out materials
involved to connect all this. Choosing a poor
material might be hazardous to the engine should
it fail. Aluminum, Copper, Rubber, PVC, and ABS
were all considered. Of all these materials, I
found PVC to be the most dangerous. UV damage,
and thin walls simply make it unusable. In the
right conditions, would warp from heat. In about
a year it would shatter/crack because of
exposure to outdoor conditions. Aluminum/Copper
was a good choice, but difficult to work with
and not very impact resistant unless it was
thick, it maybe used in a second generation
snorkel rebuild. (Fig 4) ABS was a great
choice because of the ruggedness, and all
weather spec, it was also widely available.
Rubber was also used to allow for engine
movement and vibration. 2.5” was a good size
after examining other snorkel systems with
larger engines. V-8’s can comfortably get away
with 3” system provided there is no back
pressure.

(Fig 4 – Canister
Installed)
After assembling the canister, it was obvious
where I would need to route the system.
Originally, I had conceived the idea of routing
into the cab and out in front of the windshield.
But I really disliked the idea of trying to make
that a clean seal from rain/snow. I also
considered just drawing cabin air, but found
this to be a very dangerous idea should the
engine malfunction and backfire. So I chose to
route it to the side, traditional I guess.
However, the Charcoal-Gas evaporator canister
was in the way. It was relocated to the lower
battery tray, and to my surprise, no additional
hardware was required to do so, the hoses and
wires fell into place. It was another perfect
fit. (Fig 5) You can see the evap sits
snug below the clutch reservoir and uses
otherwise wasted space.

(Fig 5 – Evap
Relocated)
Now it was obvious where the system would need
to go outside. This is more painful than it
looks and reminds you that you’re committed to
the project. (Fig 6) If you have second
thoughts, a Club sticker could cover this. Using
Masking tape minimized paint damage.

(Fig 6 – Hole Saw
Carnage)
I found Roof Flashing in Home depot makes a
perfect Bevel cover. Objective 3 was looking
good.

(Fig 7- Rubber
Flashing)
Routing it up the side wasn’t a problem,
securing it might have been. Again, looked
around and found a product called Zip-Stick.
It’s a vinyl zip-tie and is used to hang pipes,
it was heavy-duty and had bolt holes already in
place. Fastened to the windshield hinge, it
showed no movement or rattle.
(Fig 8)

(Fig 8 – Secured
and running high)
Finally, my intake is high. But now there were
more serious problems… How to keep it dry on
rainy days, what sort of water separation
method? What about ingesting tree leaves on the
trail? What about Air restrictions, should it be
a ram or risk it being vacuum? I looked
elsewhere at working solutions. Hummer desert
versions had a clever Sand/Air Separator. The
water Separator was good too. But both bulky.
ARB’s ram method was a concern too. On a rainy
highway, you can ingest a good amount of water,
it’s also allot of drag, like we need more of
that. I’ve seen some people simply put their
entire filter up there to do the work.. bad
choice too because of water exposure and filter
deterioration. I looked at my local trash truck
and saw the solution. Simply cap the intake, and
put it in a favorable area. A 4” ABS end-cap
worked well. Securing it to the pipe wasn’t
difficult either. In this configuration, I’ve
easily added pre-filters and socks over the
intake in less than favorable conditions. 4
Large notches ensures a good unrestricted
surface area for air (Fig 9) As an added
bonus, it’s aero-dynamic. Further more, it is
getting a ram-air effect off the windshield, but
not close enough to sip water from it. What more
could I want?

(Fig 9 - Intake)
The system was installed. And it worked! (Fig
10) A situation like this was a perfect
example of why it was a good idea.. our stick
test only showed this pool to be 3” of standing
water. Although not shown, the entire hood was
submerged later.

After thoughts
about this system includes rebuilding it in
Custom Aluminum tube. Additionally, maybe adding
some resonance baffle box. The sound is awesome,
you can easily hear any engine hiccup or
malfunction when it happens. However, it does
get sorta loud on the highway with the
continuous engine drone.
Conclusion - The performance is great and
it looks awesome. But you can’t stop there.
Since using the system, I’ve discovered long
term effects and damage from water exposure.
Greatest damage was the Transmission which I’m
still running. Smaller items include a whole
distributor worn beyond service, and a thrust
bearing which died long before it’s time. As
stated above, the snorkel is engine insurance,
but not a license to cross bottomless rivers.
Electrical systems are still exposed and a
Clutch can still saturate to become useless
among other things.
Hope this gives you some insight on what it
takes to build a functional snorkel system.
Please give me credit if you choose to post this
elsewhere. Thanks!
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